Topeka Runaway Disaster: Difference between revisions

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The brake line on a locomotive plays a key position in the pneumatic braking system of a locomotive. Any corrosion or damage to this line can compromise the braking system, which can lead to braking deficiencies or even a complete brake failure.
The brake line on a locomotive plays a key position in the pneumatic braking system of a locomotive. Any corrosion or damage to this line can compromise the braking system, which can lead to braking deficiencies or even a complete brake failure.
[[Category:CGTR]]
[[Category:CGTR]]
== Accident ==
At 3:35 AM, the Central Gateway Turtle Railroad's Thundering Lapis, consisting of 8 coaches containing a total of 867 passengers and being pulled by GP40FH-2 #1, would depart from {{wp|Kansas City, Missouri}}, to begin its trek to Topeka, Kansas. The train was relatively short, compared to its usual, quite large haul, due to its early departure time intended for commuters.

Revision as of 21:09, 1 March 2024

Topeka Runaway Disaster
Details
Date27 November 1994; 30 years ago (1994-11-27)
4:45 AM
LocationTopeka, Kansas
Country United States
LineCentral Gateway Turtle Railroad
CauseBrake line leak
Statistics
Trains1
Passengers867
Crew3
Pedestrians5
Deaths178
Injuries309
Damage1 GP40FH-2
8 Bi-level coaches

The Topeka Runaway Disaster was a railway accident that occured on November 27, 1994 (1994-11-27), in Topeka, Kans as, when CGTR's Thundering Lapis—containing 8 bi-level passenger coaches and being pulled by CGTR #1, an EMD GP40FH-2—would fly off of a bend at 77 miles per hour (124 km/h), crushing 2 cars, derailing all 9 cars and locomotives, and killing 178 people and injuring 309 more after losing control due to a brake line leak.

The accident was named after the city it took place in—Topeka, Kansas—and would become the most deadly train wreck in American history, surpassing the Great Train Wreck of 1918 by 77 deaths.

Background

In 1998, 6 years prior to the incident, the Central Gateway Turtle Railroad would make a strategic decision to replace EMD F40PHs #1–3 with newer models, EMD GP40FH-2s. In the eyes of the CGTR, this transition seemingly marked another upgrade to more modern and efficient locomotives for hauling their esteemed passenger trains.

Initially, the transition went quite smoothly, and the three new EMD GP40FH-2s effectively pulled the Thundering lapis for a good 6 years without encountering any significant issues. Be that as it may, in 1994, a critical oversight would occur during a routine inspection on locomotive #1.

Due to an inadequate inspection, the maintenance crew responsible for locomotive #1 would fail to identify a corrosion problem on the locomotive’s Westinghouse 26 brake line. This corrosion, which had likely developed over time due to humidity and exposure to corrosive agents, would go unnoticed.

The brake line on a locomotive plays a key position in the pneumatic braking system of a locomotive. Any corrosion or damage to this line can compromise the braking system, which can lead to braking deficiencies or even a complete brake failure.

Accident

At 3:35 AM, the Central Gateway Turtle Railroad's Thundering Lapis, consisting of 8 coaches containing a total of 867 passengers and being pulled by GP40FH-2 #1, would depart from Kansas City, Missouri, to begin its trek to Topeka, Kansas. The train was relatively short, compared to its usual, quite large haul, due to its early departure time intended for commuters.